Horizontal Stabilizer Nose ribs

Didn’t make much progress over the weekend, but I set up the cradles and skins, then started riveting the nose ribs to the skins. It’s been a while since I bucked rivets, as most of the rudder was done with the squeezer, back riveting, or pop rivets. I made a practice piece to remind myself how to do it, and to ensure I had the right air pressure at the gun. Access is a bit awkward, especially for the forward most rivets. The skins are deep enough where it’s a stretch getting a hand down inside, and near the leading edge, there’s not enough room for a hand, a bucking bar, and a rivet. I finished this step on one skin, getting the three nose ribs in (the 4th one is attached to the spar and gets riveted in later), and started on the second. I’ve got a few rivets that will need to be drilled out and redone, but I’ll worry about that once I have the whole step completed. I may end up using flush pop rivets in the forward rivet holes, since it’s hard getting a bucking bar on those rivets, and I managed to mess up a few of them.

The forward-most rivets in this rib are both bent and not fully formed. I’ll drill out and replace:

Riveted Horizontal Stabilizer front spar

I riveted the stringers to the in-board in-spar ribs and stringer web.

Then I clecoed and riveted all of the in-spar ribs to the front spar, and the two outside nose ribs. I got everything done with the pneumatic squeezer, which was easy given that I have a sheet with all the settings. Just twist the adjustable set the right number of turns and then squeeze away. These were all 4-4 rivets except for 8 4-5 rivets where the rivets go through the spar, spar cap, and then the rib.

Next step is to start riveting the nose ribs to the skins.

Finished countersinking

I finished up the Spar and stringer countersinking work tonight, everything went quite well. The only issue I had was when I tried to use the drill press for the stringers. After a lot of setup time, and lots of clamping, the piece moved slightly and I ended up with a lopsided hole. I switched back to using the drill after that mistake, as it’s easier to feel what’s happening and stop or adjust if needed. The enlarged hole will need to be drilled out to fit a larger rivet, which shouldn’t be a problem. Given that I countersunk over 400 holes, I’m ok with one error.

Then I riveted the inboard inspar ribs to the stringer web, and clecoed the stringers to the stringer web. I decided to stop there, as it’s getting late.

Countersinking

More countersinking on the Horizontal Stabilizer spars tonight. I finished the rear spar, and got about half way through one side of the forward spar. It’s getting faster, given how much practice I’m getting, but I think I still have another hour to go to finish this step.

Dimpling and countersinking

I finished deburring and dimpling the HS skins this weekend, and started countersinking the spar flanges where they will accept the dimples. It’s challenging getting a perfect countersink. The goal is to have the top of a rivet be 0.007 inches below flush. Even with a well calibrated countersink, just the slightest hand pressure difference can result in a different amount. I contemplated setting up the drill press, but opted for the hand drill where I can more easily feel what’s happening. The drill press would also be a little awkward given how long the spars are (10 feet). Everything came out ok so far, I’ve finished around 50 of ~400 holes. Once I’m done countersinking I’ll also prime the inside of these holes, as they will be contacting the skins.

Horizontal Stabilizer Skin prep

The last couple of nights I’ve spent time deburring and dimpling the HS skins. I peeled off the vinyl inside the skins, and on the outside to expose the holes. Deburring is fairly easy, the edges don’t take much to smoothen out, and the holes are all pre-punched to final size. For the holes, a quick debur with the tool is all I’m doing. For edges, I’m using my vixen file to remove bumps, then an edge deburrer, and then a small file. The combination of tools gives a good outcome. I was only able to finish dimpling one side of one skin tonight, I just can’t stay awake any longer.

Dimpling ribs

Tonight I started by addressing an over-sunk hole on the spar. I reamed the hole out to #30 size, then countersunk for a 1/8th rivet. Then I trimmed a 4-5 rivet to 4-4.5, and riveted it in place. This is the very middle rivet on the top of the spar, so it even looks symmetrical.

Then I used a beam-style torque wrench to torque the rear spar nuts to 28 inch pounds. The tool is easy to use for these low torque settings, and apparently sufficiently accurate.

Then I match drilled some holes for the inboard most ribs, then dimpled all the ribs, except for the specific holes that will take screws for the fairings etc.

Here is the forward spar with the inboard ribs clecoed on for match drilling. They are set at a 10 degree angle:

I used the squeezer to dimple the ribs. It was fast and easy.

Stack of dimpled ribs:

Riveted Horizontal Stabilizer spars

With the priming done, I was able to rivet the spar doublers, spar caps, and the hinge brackets to the forward and rear spars. With my pneumatic squeezer already calibrated (I made a chart with all the various settings), it was a fast and easy set of tasks.

I started by riveting the rear spar doubler. Here it is part way through:

Then I riveted on the hinge brackets:

Then riveted together this part, which contains a bearing:

I clamped it up to keep it square while riveting:

This bolts onto the spar, so I need to get a torque wrench to set these nuts to 28 inch pounds:

Then the forward spar. This has the spar caps, so it’s slightly different. More rivets, and longer rivets. I only got part way through before deciding to take a break for the night:

Primed Horizontal Stabilizer parts

Apart from the skin, I primed all the HS parts today. The process went a little faster and easier than before, and the results look good. I mixed 200 grams of part A, and used a little over half what I mixed up. It really doesn’t take much to coat the parts in a thin layer, and according to the manufacturer, a barely visible layer of this epoxy primer is 90% effective.

Here are some before and after pics. These parts are cleaned but not etched:

And here they are primed:

These parts are cleaned and etched:

And now primed